|
The Maricopa Live Steamers realized early on that if we were going to have
passenger and freight yards reached through a complex throat, we would need an
easy and fast way to line the switches to the proper route. There are five
branches fed by these yards and as many as ten turnouts must be lined for a
train to enter or exit correctly. Our plans called for 24 powered turn outs so
we would need to try and keep the costs down. The only throw mechanisms on the
market at that time were complicated, finely machined electric coil powered and
could not be thrown by hand unless the coil motor was unscrewed and
disconnected. We tested a pneumatic system but decided against it because of the
cost and labor involved in installing and maintaining the air supply tubing
runs, some of which are 300 feet from the interlocking tower.
One of our members came up with the idea of using old battery powered
screwdrivers that people had discarded because the batteries would no longer
hold a charge. A screw type mechanism was built and would have been fine except
for the fact that is could not be hand thrown without disconnecting the electric
drive. We then wondered if we could connect the shaft of the motor directly to
the end of the shaft of the throw mechanism. Most of us felt that this would be
impractical because it would be far too much of a strain on the small gears
inside the screwdriver. However, we welded a 1/4 inch socket directly on the end
of the throw bar shaft then using the screwdriver bit, which happened to be 1/4
inch, we connected the motor to the throw bar.
The motor had been prepared by removing the batteries, battery housing,
reversing and on and off switches. The wires that come out from the motor were
then connected to a two prong polarized plug. When the battery housing was
removed it left a nice large hole in the back of the motor housing. The machine
was then screwed down to a piece of 2 x 4 that had been connected by angle
brackets perpendicular to the throw shaft. The electric motors are D.C.
permanent magnet and are reversed by simply reversing the polarity of the feed.
The motors are rated at 4.5 volts but we have used as high as 12 volts for very
short periods and have had no problems. You would have to decide on the best
voltage depending on the length of your wire runs.
The switches can be controlled either electrically from the tower or throwing
the bar by hand. In the event of a burnout or other problem, the switch motor
can be unplugged and changed in a matter of minutes. Even though it’s difficult
to believe that this system would be practical, many of our machines are now in
their fourth year of operation with over 3,000 throws and are still working
reliably.
|